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my69opelgt

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  • Posts

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About my69opelgt

  • Birthday 03/28/1984

Contact Methods

  • MSN
    my69opelgt@gmail.com

Profile Information

  • Gender
    Male
  • Location
    hayden, idaho
  • Interests
    Wrenching, driving, music :)
  • Occupation
    Fabrication/Welding technician @ Scottco Distributors
  • Referral
    Crystal Kerr
  • Biography
    i was raised by a bodyman and been working on cars since 10
  • Vehicles
    looking for ea82 sedan/wagon again

my69opelgt's Achievements

Advanced Member

Advanced Member (3/11)

11

Reputation

  1. Half the thread pics are broken links, what happened?
  2. that is a sweet 90 lego. mine needs much more work lol

  3. We should start a local legacy group with the three of us :) what do ya say?

  4. Hello. nice to meet you. how is the mazda doing?

  5. I feel it would be fair to leave a message saying hello at this point. Seeings as how we've met now. =]

  6. thanks for helping me out last night man. ill be done by this weekend and hopefully be driving it again.

  7. EVER HAVE SOME ONE LIE TO YOUR FACE? I PAID 500 BUCKS FOR A 200 POUND BOAT ANCHOR!!!!!!!!!!!!!!!!! LAST year i bought a " Rebuilt motor" from a fellow USMB member in portland. He claimed it ran but wouldnt idle due to stage 3 cams plus the stock ecu wouldnt work with that large of a cam. so i got a 1)"rebuilt motor", 2) t3/t4 turbo, 3) custom uppipe, custom down pipe, 4)external wastegate, 5)xt manifold, 6)and a rx awd d/r locking center dif transmission. I took the cams off and put on n/a cams. replaced h/g and oil pan gaskets. traded the turbo for a medium sized one lol, and put it in. now it started but i could not get it to stop spewing oil out the crank case vent. so i tore it all down AGAIN. found the reason.... now i know there are always a risk when buying used parts. i just cant believe he never noticed the piston slap or the gap in the rings! i took it to a certified mechanic shop and was told the cylinders were bored .30 over!!! but the crazy part is he put standard pistons back in!!! the block was ruined ofcourse cus it was bored untill the water jacket showed in the cylinder wall. so i call this guy and ofcourse he wont answer me. im upset but i just wanted to get the whole truth from him of why he did it. maybe he had some one else do the machining and didnt know? idk but now im using an old block that was pulled from another gl-10, 207k miles but it checked out ok. using the best heads of the two motors and new gaskets. I wont say it was worth it just for the custom pipes and tranny cus i could have avoided wasting two months and two sets of head gaskets on the bad block. live and learn.
  8. hey do you have a NA short block lying around?

  9. Now that you mentioned it i think that it is very odd to get a reading on the temp gauge even when no coolant is in the rad. About the oil drain... thank you i already know it has to face down and it does now. old pic lol. I have the motor out and apart already, i must have been tired when i put it together the first time cus i found RTV on the intake gaskets oops. i think that plus the cheap gaskets were the cause for taking on coolant. I bought FELPRO TORQUE-MATIC HEAD GASKETS, But only one had the oil passage rubber o ring, the second was completely blank. i went back and they couldnt get another felpro with the ring. So i hope the ALTROM GROUP gaskets will be ok. they claim to be one of the oe suppliers for subaru in japan.
  10. Here is a quick phone vid

    ill have a better one up in an hour

  11. Here is a video from my phone. ill have a better vid up in a hour

  12. Here is a quick video from my phone, crappy i know, as it sits today. was able to get a longer stud but it felt like it was not gonna hold so i left it snug. I am in the process of uploading a higher quality video and will post that link when it finishes. Ok here is the new high quality vid. Enjoy http://www.youtube.com/watch?v=HSiQka3mt4g
  13. K so i found i had an exhaust leak on the d.s. head, its missing a stud thus stripped out somewhere. so it only boosts to 4-5 psi. it was running ok even with the leak but then a few days of driving to work and back it started losing coolant and warming up. i would add coolant and by the time i get home its gone! like magic! Ive drove the car with an empty radiator unknowingly but yet it did not once over heat... im sure if i had been wot all the time it would have though. it has dual electric fans so im thinking that is just barely enough to air cool it? So i made a noob mistake by putting cheap egay gaskets on it the first time around. im picking up FELPRO head gaskets and OEM intake and cam carrier seals to hope fully fix my problem. One unusual problem that is concerning me alot is when it takes all that coolant, it gets pulled into the oil, and then the oil psi is too much and it pushes out the turbo seals and sucked through the intercooler and into the motor. im pretty sure this is a bad thing to happen. will it be fixed by replacing the HG?
  14. lol ya thats what i told les schwab too. all they would finance me is the stock sized all season.
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