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tizzle

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Posts posted by tizzle

  1. I started a thread about the exact same problem a couple weeks ago.

     

    http://www.ultimatesubaru.org/forum/showthread.php?t=28929&highlight=rx+jerking

     

    I did several things. Turns out the timing was way off, and 2 of the spark plug wires on the distributor had the connections receded into the boot. I fixed that and it made a large difference, but the problem still persisted slightly.

     

    Then I ran 2 different fuel system cleaners as well. This also helped.

     

    I also replaced my fuel filter which was nearly brand new, problem still not solved entirely. ... I'm thinking that the fuel pump may solve the problem completely.

  2. 2000 degree titanium colored satin coat. Just sounds pretty.

     

    DSC00603.jpg

     

    DSC00584.jpg

     

    Got the headers on yesterday. I don't know how Will did this in 15 minutes, because it took me a very long time. I had to replace the turbo cooling hoses with longer ones due to the new placement of the turbo, but luckily I have extra hosing sitting around.

     

    I also did a port/polish on the extra turbo I had sitting around. So part of the time I spent was on replacing the turbo.

     

    The results I'm very happy with. Definitely more power, and in places where it never existed before!

     

    So now I gotta figure out how to finish of the exhaust system, and put the downpipe on.

     

    ---todd

  3. This happened to me. It was the worlds biggest pain. We spent a good couple days, heating it, spraying it, hitting it, prying it, and swearing at it. Tried an easy out CAREFULLY, yet unsuccessfully, but It looks like you got that stuck, which makes the way we finally got it off difficult. WE just kept slowly drilling down that bolt, until the intake manifold had almost no bolt left to stick to, good luck, i feel your pain.

  4. Ok, haven't been able to check in often due to a fried hard drive:banghead:. But I figured out the problem. I messed with the distributor. Turns out I had done the ignition timing very wrong. I'm an idiot, and also 2 of the connections int the wires were receded into the boots. But now the ignition is all set to stats, and the RX is running very pretty. It still has a very slight jerking, but not very noticeable. I rechecked the codes, and got abnormal o2 sensor, and something about the wastegate I think, 32 and 44.

     

    anyways, thanks guys

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