GeneHacker Posted July 31, 2006 Share Posted July 31, 2006 My 2.2 98 legacy was hesitating a little bit at low rpms so I figured I would give it a tune up. I replaced the air filter, plugs and wires. When I started it, I sounds fine...but after 20 seconds it stalls. I can keep it running if I rev it but it runs like crap...and eventuallys stalls. It smells like its running really rich. I double checked the plugs (gap, torque) and the new wires...everything looks fine. I cannot figure out what would be causing this. Any thoughts?? Thanks Gene Link to comment Share on other sites More sharing options...
Olnick Posted July 31, 2006 Share Posted July 31, 2006 Hi, Gene. (I just love saying that--it sounds so . . . clean!) How many miles on your car? How does it smell like it's running rich--raw gas smell or excess exhaust smell? Have you checked for codes? Might consider replacing your fuel filter if it hasn't been done in awhile. PCV valve too. Also might need to replace the engine coolant temperature sensor and/or the O2 sensor. But I'd start by checking (with an OBDII scanner) for any stored codes. That might point you to a specific problem. Good luck. Link to comment Share on other sites More sharing options...
cookie Posted July 31, 2006 Share Posted July 31, 2006 A lot of time folks knock off a critical vacum hose when doing a tune up. Link to comment Share on other sites More sharing options...
Manarius Posted July 31, 2006 Share Posted July 31, 2006 Could be vacuum line, could be Coolant Temp. Sensor, could be fuel filter, or it could be the MAF (I had this problem ). I'd check them in that order as well. Do you have any hard starting problems? If you get it to move, does it stall out while you're moving? As I read more and more into your problem, I think you have a broke MAF - assuming you have a MAF. Before going straight for a MAF though, I'd check fuel filter and coolant temp sensor. Link to comment Share on other sites More sharing options...
GeneHacker Posted July 31, 2006 Author Share Posted July 31, 2006 Yea, there was a hose that got knocked off under the intake. I reattached the hose and its running great. Also the low RPM hesitation seems to be fixed as well...looks like the tune up did it! Thanks for the help!! Link to comment Share on other sites More sharing options...
cookie Posted July 31, 2006 Share Posted July 31, 2006 don't ask us how we know you can knock that hose off..... Link to comment Share on other sites More sharing options...
Olnick Posted July 31, 2006 Share Posted July 31, 2006 A lot of time folks knock off a critical vacum hose when doing a tune up. Way to go, cookie! Link to comment Share on other sites More sharing options...
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